Rivne NPP Unit 3 with WWER -1000/В‑320 reactor is under operation since
1986.
22 September 2009 was 118th
day of Unit 3 planned outage that started on 28.05.2009. Reactor installation
was in hot shutdown state, primary circuit temperature - 280°С, pressure - 160 кg/сm2. The core was in subcritical state,
concentration of liquid neutron absorber (boric acid solution) was a “shut
down” one - 16 g/kg, all control rods were inserted into the core.
Equipment of primary and secondary
circuits and containment were sealed. All three safety channels were in
stand-by mode of operation.
On 22.09.09 planned testing of pressurizer safety relief
valves was started.
Note: The pressurizer safety relief valves
are designed to prevent overpressure of the primary circuit under
transients with fast turbogenerator load reduction. Valves consist of 3 main
valves and 6 pilot valves (two for every main valve). In case of increasing of steam
pressure in pressurizer up to 185..192 кg/сm2, pilot valves are opened that results in
opening of the main valves for 5¸10 seconds and decreasing of primary circuit pressure to set point of pilot
valve closure (176..180
кg/сm2).
By design, steam is
released to the relief tank for condensation and returning back to primary
circuit.
Pressurizer safety relief valves,
produced by German company «Sempel AG» were installed
at Unit 3 in
1986 when unit was put into operation. Such valves are operated successfully at
9 of 15 Ukrainian units.
Overhaul maintenance of all
pressurizer safety relief valves was conducted
during planned outage in 2009. After completion of maintenance, in accordance
with the unit technical specifications and design documentation, correctness of
their work shall be tested by actual pressure increasing with short-term steam release to relief tank.
Event sequence:
The tests started according to
standard “Testing program. Primary circuit excess pressure protection system.
Safety protection system. Testing of pressurizer safety relief valves by
pressure increasing up to actual actuation. Unit 3” 141-70/3-PR-CNIO on 20:45 22.09.09.
After primary circuit pressure
increased up to 185 кg/сm2, pilot valve is opened (21:14:49), pressurizer main valve is opened (21:14:50) and primary circuit pressure started to drop.
However, main valve is not closed under pressure 175 кg/сm2 (21:15:00)
although interlock on its closure was actuated on-time.
Due to long-term steam release from
pressurizer, pressure and temperature in relief tank started to increase and
under pressure of 12 кg/сm2 membrane that protects relief tank from
destruction was ruptured. From this moment coolant from primary circuit started
to leak to containment (as a steam and as parameters go down, as a steam-water
mixture). In such a way, integrity of primary circuit – the third barrier on a
way of radioactive substances and ionizing radioactive sources, was broken.
According to technical
specifications, personnel stopped to fulfill testing program and switched on
ECCS high pressure pumps in order to compensate loss of coolant due to leak to
containment through pressurizer safety relief valve and relief tank.
On 21:49:13 containment pressure reached 0,3 кg/сm2 (differential) that actuates spray channels of safety systems. In total,
they work during 3 hours 40 minutes and as a result, equipment of primary
circuit (reactor vessel, lid, main circulation pipelines, steam generators,
pressurizer) were sprinkled by cold radioactive coolant (solution of potassium
metaborate).
The last protective barrier –
containment – functioned as designed, that is why radioactive coolant was
localized within containment and there were no releases to the NPP site and the
environment. After condensing and cooling, coolant run off to the containment
sump and pumped to the primary circuit by ECCS high pressure pumps.
On 22:29, because of injection of cold boron water to primary circuit by ECCS high
pressure pumps, its temperature decreased to 82°С, pressure - to 35 кg/сm2. NPP personnel started to compensate loss of coolant by ECCS low pressure
pumps. Primary circuit pressure was decreased
to atmospheric one, level dropped below joint of pressurizer safety relief
valve. Leakage was stopped.
On 16:05 23.09.09, after pressure and temperature decreasing,
conduct of radiological survey and getting SNRCU resident inspectorate permission,
NPP personnel along with representative
of SNRCU resident inspectorate walked down to containment and confirmed that
incident had been caused by failure-to-closure of the pressurizer safety relief
valve YP21S01.
On 23.09.09 NPP management, according to procedure, sent to SNRCU
preliminary information about reporting event at NPP.
Provisionally NPP rated the event as «P07» category (failures of group “B” safety related equipment) and with level “0” under INES scale (deviation, no safety
significance). However, on 24.09.09,
preliminary analysis of event sequence conducted by SNRCU resident inspectorate
proves that the following deviations from
normal operating conditions and design modes took place:
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Violation
of safety limit on minimal pressure departure from primary coolant boiling;
-
Violation
of safety condition (pouring boric acid solution on dividing bellows and studs
of main reactor joint);
-
Violation
of operating limits of safe operation (surpassing permitted cooling down rate
and pressure decreasing rate in the primary circuit);
-
Thermal
shock of reactor vessel metal due to injection of cold boric acid solution to
primary circuit.
On 25.09.09, taking into
account the above, the Chief state inspector of Ukraine on nuclear and radiation
safety required from the Ministry of Fuel and Energy of Ukraine, SE NAEK
“Energoatom” and Rivne NPP the following:
-
Re-rate the event with category «P02» (violation of limits and/or
conditions of safe operation, not developed into accident);
-
Correct
the event INES rating (violation of barriers integrity);
-
Perform
comprehensive analysis of transient at reactor installation and reveal all
violations of system and components operation;
-
Develop
and agree with SNRCU programs and methodologies on examination, inspection, monitoring and confirmation of capabilities of reactor
installation equipment;
-
Substantiate
possibility of further safe operation of Unit’s safety related systems and
components and agree the substantiation with physicometallurgical and design
organizations including OKB “Gidropress” (main designer of reactor
installation) and TVEL Corporation (fuel supplier).
Further, SNRCU department of nuclear
installation safety assessment, performing assessment of transients in the
course of liquidation of the event consequences, set the following:
1) The mode had serious potential danger because
during periods of time 21:21 ¸ 21:47 and 22:33 ¸23:24 (when NPP personnel made attempts to manually fill in pressurizer and control
primary circuit pressure by three ECCS high pressure pumps) pressure difference
in secondary and primary circuits was 15¸30 кg/сm2. In case of leakage of steam generators heat-exchange surface (that is very
probable under such hard cool down conditions) it may lead to entry of “plug”
of distilled water (instead of boron water) to the core and generation of local
criticality zones.
To fix this known safety deficiency
of reactor installation WWER‑1000/B-320,
a
branch measure “Modernization of ECCS HP to control outlet pressure of pumps
suppling water to primary circuit” was developed and agreed by SNRCU. This
measure was developed in the framework of the “Concept for safety improvement
of operating NPPs”. However, its timely implementation on “pilot” Unit 5 of
Zaporizhya NPP in 2009 was frustrated and its
implementation at the rest units WWER‑1000/B-320 in 2010 is very doubtful. SNRCU
repeatedly informed the operating organization and the Ministry of Fuel and
Energy of Ukraine about this situation.
2) Fortunately, in accordance with the “Concept for
safety improvement of operating NPPs” and pursuant to SNRCU requirement,
replacement of thermal insulation of all primary circuit elements in
containment was completed in 2009. It was mitigating circumstance because old
insulation could be disintegrated under impact of increased temperature and
humidity and could enter into primary circuit and ECCS channels. This
circumstance simplified liquidation of incident consequences, further repair
and recovery works, allows to save all three safety channels and prevent
chokage of equipment and fuel. Exactly this circumstance became a decisive one
in the course of examination and cleaning of equipment (only 57 days of off-schedule
outage was requested; duration of unplanned outage in case of similar event at Zaporizhya Unit 1 in 1995 was 78 days).
Liquidation of incident consequences:
According to SNRCU requirement,
considerable amount of work has been conducted at Rivne NPP Unit 3: full
unloading of the core, examination of fuel, metal of reactor vessel, lid and
internals, main circulation pipeline, steam generators, pressurizer, main
circulation pumps, control and protection system, inspection and cleaning of
three ECCS channels.
On 06.11.09 SNRCU received a reply from representative of «Sempel AG» and the first
version of report on reported event at Rivne NPP Unit 3. The operating
organization, on SNRCU insistence, rated the event with INES level «1» (anomaly) and with «P02» (violation of limits and/or conditions of safe operation, not developed
into accident).
Preliminary assessment of materials
revealed that spare parts for pressurizer safety relief valves were ordered and
manufactured at factory of corporation “Kyiv valves” in 2005 without approval
of technical specifications by producer of pressurizer safety relief valves (violation of par. 1.2.6 «Rules on arrangement and safe operation of
equipment and pipelines of nuclear power installations» PNAE G-7-008-89). According to report of «Sempel AG» representative, geometrical
dimensions and chemical composition of slide valve do not meet «Sempel AG» requirements.
In the course of testing it resulted in decreasing of a gap between slide valve
and guide bush and, finally, it led to pilot valve jam in opened position.
In addition, it was established that
installation of the valve parts during outage in 2009 was conducted with
violation of maintenance procedure (relevant technical decision on replacement
was not documented properly).
On 11.11.09, taking into
account the above, the Chief state inspector on nuclear and radiation safety
returned back the event report №3ROV-P02-002-09-09 for
additional investigation,
pointing out to absence
in the report correct root and direct causes as well as absence of corrective
measures for all units of Ukrainian NPPs.
On 08.11.09 SNRCU received additional materials from
the operating organization and on 19.11.09, based on
analysis performed by the State scientific and technical center on nuclear and
radiation safety, set forth additional requirements regarding substantiation of
steam generators integrity (in particular, welded seams №111), pointed out to low level of safety culture
(violation of par. 5.3.4
«General provisions of
nuclear power plants safety» (ОPBU-2008)) and requested the following:
-
Develop
and submit to SNRCU relevant branch-level measures to prevent usage of
inappropriate parts for maintenance and repair safety related systems;
-
Bring
to administrative and/or disciplinary responsibility managers of NAEK
“Energoatom” and Rivne NPP, whose actions or inactivity led to failure of the
pressurizer safety relief valve at Rivne NPP on 22.09.2009 and to violation of
regulations (ОPBU-2008 and PNAE G-7-008-89);
-
Perform
during next unit outages onetime inspection
of primary circuit excess pressure protection
system and secondary circuit excess pressure protection systems (steam
generator safety relief valves, fast-active steam discharge valves to atmosphere);
-
Perform
onetime direct and full functional test of abovementioned equipment according
to par. 6.2.27 PNAE G-7-008-89, par..10.4.3 NP 306.2.141-2008.
Currently Unit 3 of Rivne NPP is in
cold shutdown state.
Temperature of primary circuit
coolant is 50°С, pressure – 10 кg/сm2. The core is in subcritical state, concentration of neutron liquid
absorber is 16 g/kg.
To demonstrate design
characteristics of safety related equipment, tests of systems and components
were started according to methodologies and programs and under approval of
SNRCU resident inspectorate.
The first package of documents
submitted to SNRCU by operating organization to substantiate Unit 3 safe
operation is under expertise at the State scientific and technical center on
nuclear and radiation safety.
The inspectorate will issue a
particular permit to Unit 3 start up (including reactor installation heating up
and bringing to minimum controlled power level) on special “start-up” meeting
provided all abovementioned SNRCU requirements are fulfilled.
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Date, time
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Event chronology
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22.09.2009
20:45
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According to the pressurizer testing program,
the main circulation pumps (MCP) 3YD10,20,30,40D01 are switched off. Setting «DTs < 10°С» of
the emergency core cooling system (ECCS) protection is deactivated.
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|
20:46
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Pressurizer heaters are switched on in order
to increase pressure in primary circuit.
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21:14:49
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Primary circuit pressure reaches 186,5 kg/сm2. By signal of the control scheme electromagnets of pilot valves (PV) 3YP21S03, S04 are
switched off and main valve (MV) 3YP21S01 is opened.
|
|
21:15
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Primary circuit pressure is 175,7 kg/сm2. Electromagnets of PV 3YP21S03,
S04 are switched on
and indication of MV 3YP21S01 closed position is appeared but pressure in
the primary circuit keeps decreasing. Taking into account decreasing of
primary circuit parameters and raising parameters in the relief tank, the MV 3YP21S01
failure to close is identified. Attempts to close 3YP21S01 are not
successful.
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21:15:47
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By interlock signal all pressurizer heaters
are switched on.
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21:16
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By interlock signal “containment pressure
> 0,003 kg/сm2” isolation valves of ventilation systems TL 22,42 are closed.
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21:17
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Pressurizer heaters are switched off by
interlock signal “pressurizer level < 4200 mm”.
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21:18
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Shift personnel switch on pumps TB10D02,03 to supply boric acid from ТВ-10 tanks to inlet of primary circuit charging (makeup) pumps.
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21:19
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Primary circuit pressure is 66 kg/сm2. A protection signal «DTs < 10°С» is
generated without impact on ECCS actuators.
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21:20
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Primary circuit pressure is 58 kg/сm2. Opening of check valves on
pipelines from ECCS hydroaccumulators 1-4 to primary circuit is noted.
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21:21
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Primary circuit pressure is 50 kg/сm2. Control room operators switch on
pumps TQ14-34D01, TQ13D01 connected to primary circuit.
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21:26:22÷
21:29:25
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In order to close
3YP21S01, valve 3YP21S08 was opened
and electrical power was supplied to electromagnet for opening of valve 3YP21S09 for
short period of time. The valve 3YP21S01 was not closed.
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21:30
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To cool down reactor installation, filling up
of steam generators 1-4 is started.
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21:34
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Primary
circuit pressure is 48
kg/сm2. The control room operators switched on the
pump TQ23D01 connected to primary circuit.
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21:37
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Shift personnel closed 3YR60S01,02 and by opening 3YR01÷03S01, 3YR11÷41,12÷42S01 and 3YR51÷53S01 connected together emergency gas-off lines
from reactor, steam generators 1-4 and the pressurizer (with discharge to the
relief tank).
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21:44
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Primary
circuit pressure is 44 kg/сm2. Control room operators switch on
pump TQ33D01 connected to primary circuit.
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21:49:13
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Containment pressure >0,3 кg/сm2. It is noted
that ECCS protection is actuated, containment is localized by closure of
isolation valves, ECCS
mechanisms 3TQ12÷32D01 are switched on, sprinkling solution is
injected to containment by 3TQ11÷31D01 pumps.
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21:50÷21:55
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Primary circuit pressure is 70 kg/сm2.
Pumps 3TQ14÷34D01, 3TQ33D01 are disconnected from primary circuit.
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21:55
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Primary circuit pressure is 60 kg/сm2.
Pump 3TQ23D01 is disconnected from primary circuit.
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22:13
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Primary circuit pressure is 31 kg/сm2. Pump 3TQ13D01 is disconnected from primary
circuit.
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22:30
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Primary circuit pressure is 23 kg/сm2. Boric acid supplying to primary
circuit by pumps 3TQ12÷32D01 is noted.
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22:37
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Primary circuit pressure is 22 kg/сm2.
Pump 3TQ22D013 is disconnected from primary circuit.
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22:39
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Containment pressure 0,1 kg/сm2. Pump 3TQ31D01 is
switched to recirculation mode.
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22:50
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Containment pressure 0,1 kg/сm2. Pump 3TQ21D01 is
switched to recirculation mode.
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23:10
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Decreasing of hot legs temperature below 70ºС is
noted.
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23:19:38
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Fast-acting valves
3YT11÷14S01, 02 on
pipelines connecting ECCS and primary circuit are closed.
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23.09.09
00:39
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Primary circuit pressure is 23 kg/сm2. Pump
3TQ32D01 is
disconnected from primary circuit.
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01:30
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Containment pressure is 0,03 kg/сm2. Pump
3TQ11D01 is switched
to recirculation mode.
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01:40
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Reactor installation parameters: primary
circuit pressure - 20 kg/сm2, temperature
- 50ºС, containment pressure - 0,07 кгс/см2, concentration of boric acid
solution - 20,9 g/кg.
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02:50
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Ventilators 3TL01D01,
D03, 3TL04D02 are
switched on to remove heat from containment
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03:30
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Isolation valves of containment radiation monitoring
system are opened.
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05:05
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Isolation valves of containment hydrogen
concentration monitoring system are opened.
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05:20
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Emergency and planned cool down header TQ40 is
connected to primary circuit; pump 3TQ22D01 is switched on to cool down primary
circuit, pump 3TQ12D01 is switched off.
After pressurizer level decreasing, coolant
release to the relieve tank through opened valve 3YP21S01 is stopped.
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